28th Sep 2008 Sun 0500hrs – 1500hrs
Attend to Vessel at Singapore anchorage.
Inspection of Inert gas’s cooling tower
- Found that Inert gas’s cooling tower is impossible to remove vertically from the top, because the Nitrogen generator room was located right above to it.
- Some measurement made, we recommend removing the wall at the exit door so that the Inert gas’s cooling tower can remove horizontally from the side.
- Understand that the vessel will be going for dry docking next year. So we suggest that this work to be carry out during dry dock, as it is a big project and also time consuming.
Recommened Service
Service the vessel on next dry dock.
- Overhaul all the 9 pcs. of actuators.
- Overhaul the Positioner for the Capacity’s valve and ATM‘s valve.
- Calibration for the O2 Analyzer.
- Calibration the control circuit and commissioning for the system.
- Change the Ignition transformer.
- If the Ignition Burner is bad, renew it to the remove able type.
4th Sept 2009 Fri 0700hrs to 1800hrs
Left Singapore for Hong Kong to Shekou.
5th Sept 2009 Sat 0700hrs to 1800hrs
Supervision yard fitter to dismantle of cooling tower.
6th Sept 2009 Sun 0700hrs to 1800hrs
Waiting for yard fitter to dismantle of cooling tower.
Vessel dry docking, left vessel to Hotel
7th Sept 2009 Mon 0700hrs to 1800hrs
Cooling tower was brought out from the Inert Gas room, and cooling jacket was separated, demister and wet filter was in very bad condition.
Instruct the yard’s Engineer how to install the new cooling jacket.
8th Sept 2009 Tue 0700hrs to 1800hrs
Left Shekou to Hong Kong for Singapore
14th Sep 2009 Monday 0600hrs – 1800hrs
Left for Airport in morning for flight to Hong Kong.
Reached Hong Kong Airport, due to our luggage was delay we took 1630hrs transfer ferry to Shekou and meet up with agent to make visa for the custom.
We were told that Shekou was having typhoon, once we reach the hotel.
15th Sep 2009 Tuesday 0600hrs – 1600hrs
Due to typhoon, we are unable to go to the shipyard to attend the vessel.
16th Sep 2009 Wednesday 0600hrs – 1900hrs
Prepare and board the bus at hotel to shipyard for vessel.
Go to the shipyard pass counter to make working pass.
Overhaul all the IG valve actuator O-rings and solenoid O-rings
Install new temperature switch for (TS191)
17th Sep 2009 Thursday 0600hrs – 1900hrs
Attend vessel in the morning as usual.
Connect up all piping for the all the actuator except for ATM’s valve, will only back by afternoon.
Install the new 12V transformers to the system.
Dismantle the Fuel Oil Control regulator for overhaul and replace new diaphragm and oil seal.
The wet filter and demister was installed back by the shipyard staff.
Found that the blower‘s impeller was unable to move after it installed by the shipyard’s staff and told them to dismantle out to repair again.
18th Sep 2009 Friday 0600hrs – 2100hrs
Board vessel in the morning and found that the blower’s impeller was installed back by the ship’s staff.
Found that the ATM valve’s positioner was fault and renew with new positioner and back to working condition.
Found leakage from the instrument pipe line and tighten up the leakage connection.
Make calibration to the ATM’s valve and Capacity’s valve.
Tested alarm for cooling tower Lever switch, Temperature Switch and both blower temperature switch and found that working.
Due to the sea water pump are not ready, we are told to run the system tomorrow morning once the sea water is ready.
19th Sep 2009 Saturday 0600hrs – 1900hrs
Board vessel in the morning, run the Sea water for Cooling tower and found the pipe was leaking and repair back by shipyard staff.
Run the system and found that the ignition cannot fire, so change new ignition nozzle and found able to fire.
While running the system, the oil pressure drop cause low pressure alarm (PAL185) so we increase the pressure back.
Found that the sea water drain valve contact switch was cut off which cause the system to stop, due to the drain valve having vibration and the contact switch was unable to have good contact.
The sea water to DWS was insufficient; however it still able to maintain the water level of the DWS, there is a spare pressure switch (0.7bar) at the cabinet beside the I.G cooling tower it can be replace for the faulty pressure switch for the DWS by the Ship’s Engineer and remove the by link wire at main panel Terminal L1 (43, 44).
Testing the safety switch with the DNV surveyor, we tested alarm for cooling tower Lever switch (LAH183), Temperature Switch for cooling tower (TAH191, TAH192) and both blower temperature switch (TAH188, TAH190) and DWS level switch (LAL194) found in working condition.
Two push button was faulty and will be supply to the vessel from Singapore.
We run the system again, found that the O2% content control is stable, but the system stop again, because temperature was high in the cooling tower cause alarm (TAH191) due to insufficient sea water supply to the cooling tower.
We left vessel to hotel.
20th Sep 2009 Sunday 0900hrs – 2000hrs
Left Shekou to Hong Kong for Singapore.
17th July 2009 Fri 0700hrs to 2400hrs
Left Office to Airport for Sri Lanka Colombo and arrive Galle port joint vessel at the late evening.
18th July 2009 Sat 0000hrs to 0300hrs
The sea weather are bad, the Boat was swelling at ship side 6 meter by reading the ship depth marking. Finally I make a calculation and make a good jump and I was life up to vessel safely. Feeling like Disney land bumpy jump.
18th July 2009 Sat 0700hrs to 1800hrs
Working on the system as follow:
IZUMI FA2 J PLC CPU showing “Error” message, using external Computer and IDEC interface connection cable with IDEC WindLDR program online to reset and clear the “Error” message in CPU. Tested the PLC CPU and found it is in normal working order. System starts and found good.
The Inert Gas Common Alarm to Ship System alarm not working and rectified.
Tested and found alarm delivery to ECR ship alarm system panel working normal.
19th July 2009 Sun 0800hrs to 1800hrs
Sea water valve inlet scrubber always in open position and flashing led on CCR Main penal. Checked and rectified the problem.
20th July 2009 Mon 0800hrs to 1800hrs
Start Inert Gas Plant, Sea water valve inlet to scrubber open automatically. Run Inert Gas to deck and top up deck pressure. And after system stop Sea water inlet valve close automatically, no flashing led on main panel.
Inert Gas Common Alarm to Ship System alarm tested and found working satisfactory.
System left in normal working condition.
21th July 2009 Tue 0800hrs to 1800hrs
Helping Chief Officer to repair the pneumatics controller of the COP system. After the service of those controller with the Ship’s Officers and Pump man, the 3 valve can now be operate from the CCR panel.
22nd July 2009 Tue 0800hrs to 1800hrs
Left vessel when she pass by Singapore at afternoon.
17th July 2009 (Friday) 1000hrs (SIN) – 2100hrs(Jakarta) – 1 Service Engineer
Preparing tools and standby for the update from Superintendent Mr. Francis
Travel from Singapore to Jakarta and meet up with agent to hotel at 2100hrs.
Meet up Superintendent Capt. Yusra, at the hotel and discuss problem of the IGG.
18th July 2009 (Saturday) 0700hrs to 2000hrs (Jakarta) – 1 Service Engineer
Meet up the agent with Superintendent Capt. Yusra in the morning and set off to REDECO, PETROLIN UTAMA (Jakarta), where the vessel docking for discharging.
Attended the vessel and meet up with Chief Engineer, discuss with him the problem.
Replace the Output card, and run the system and found the system running satisfactory.
Adjust the cooling Jacket pressure to acceptable pressure.
Checked the Inter-lock for acceptable O2% contain to open to deck for OK.
Safety alarm switch checked found OK.
According to Chief Engineer that the demister for DWS and Scrubble are in working condition.
Explain to Chief Engineer the faulty check for the Output control card for errors.
Go through with Chief Engineer what to check before start the system and during operation.
Left vessel with the agent to hotel, and will left hotel tomorrow to airport for Singapore.
11th September 2009 (Friday)1800hrs – 12th September 2009 (Saturday) 0900hrs.
Preparation for equipments and spare parts and left office to Marina South Pier to board launch to Difko Chaser.
Capacity control circuit checked and found PR2289A was faulty and renew and circuit checked and calibration made.
Fuel oil control circuit checked and adjustment made.
Blower 1 & 2 capacity load calibrated on PR2279.
O2 Analyzer calibration checked and found normal.
Start system on auto station and found system working satisfactory with Ship’s Engineer.
23rd September 2009 Wednesday 0900hrs to 1900hrs
Left office to Marina South Pier for vessel.
Found out from electrical officer that the system was unable to run full capacity.
Test the signal from the main panel found signal in working condition, but the valve was not open/close accordingly.
Found that the blower outlet valve actuator air leakage, so cause the valve able to operate properly.
Dismantle the blower outlet valve actuator, found it was previously repair by other party and was not install back properly, as shaft clip of the actuator was not in place, and one of the actuator bottom O-ring was missing.
The actuator repair kit spare which the vessel has was wrong size, so we will get the correct size of to overhaul the actuator.
24th September 2009 Thursday 0700hrs to 1900hrs
Prepare O-rings for the actuators in the morning and board the vessel.
Overhaul the both blower outlet valve actuators and insert air to test found it open/close smoothly in the workshop.
Installed Temperature switch and Level switch for scrubber tower and alarm test found working.
However, there is insufficient instrument air and sea water pump was also unable to run, so we are unable to test the system and will come back to test the system once everything back in order.
25th September 2009 Friday 0900hrs to 1800hrs
Informed by Superintendent in the morning that the instrument air and sea water pump is back to working condition.
Left office to the vessel.
Found that the ATM valve Actuator was not working, so dismantle for overhaul and found back to working condition.
Run the system in flue gas mode, found that the blower 1 outlet valve’s positioner was not working and new position was replaced and found it back to working condition.